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December 2010
05.12.2010: I am back from my holidays, and on my
project again. Next week I will do the first 25 hrs maintenance, in
parallel I can now finish all the paperwork for the final certification.
I have tried over the last few weeks to find a noise certificate from a
SportCruiser with the same engine / propeller combination, but without
success. This means that I will have to make the noise measurement next
spring during one of the EAS measuring campaigns.
12.12.2010: Unfortunately I did not consider my job in my
plan to do the first 25 hrs maintenance. Since I returned from my
holidays I have already been back to Australia for a week, and I am
right now sitting in the plane to go there again. My plan now is to do it
on the 20th December. I will also finish all the paperwork over the
Christmas Holidays.
21.12.2010: Today I finally went to the airport to do the
first 25 hrs maintenance ceck on my SportCruiser. Before I could start,
however, I updated the software of all the Dynons on our club's
SportCruiser HB-WYC. It still had version 5.1.1, and the current one is
5.4. Some pilots were reporting communication errors between the
different Dynon units during flight, so let's see whether this cures the
problem. I also created a locked setup on the D-120 to prevent the
club's members from reconfiguring it to their individual tastes. I will
do the same on the D-100, but our OPS guys first have to tell me how
they want it to be configured. The whole story took me a few hours, so I
could only start working on my plane in the afternoon.
First Silvan told me to check the Rotax website for updates of the
maintenance manual, and indeed there is a new edition 2, revision 0,
dated July 1st 2010. Contrary to the previous edition 1, Rev. 0, the 25
hours maintenance is now identical to a full 100 hrs check. That meant
that I of course did not manage to finish everything in the remaining
few hours of the afternoon, so I will be back tomorrow.
.
22.12.2010: Even though it was not planned I spent a few
hours this morning finishing the 25 hrs maintenance check. Everything
went well and also looked. The oil filter, oil reservoir and magnetic
plug show no significant traces of metallic chips, and also the exhaust
does not show any cracks. A number of SportCruiser builders had cracks
in their exhaust, but mine seems not to be from the affected lot. As it
was not planned that I return today I could not finish all the
paperwork, but I did do the post maintenance engine test run, which went
perfectly well. I will return during the Christmas Holiday to finish all
the paperwork.
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